IronBeltKen
Lazy Daydreamer
I'm definitely not the first to attempt this - several others have successfully motorized the Walthers dumper and have the Youtube videos to prove it. Of course, all the ones I've seen up to now seem to be for the 1990's and later, where unit trains of identical-length Bethgons [equipped with with rotating couplers] are used - this allows the cars to be dumped without being disconnected from the train, enabling total hands-free operation. My era (1969-72) pre-dates that; my coal trains consist of standard 70-ton 3-bay hopper cars built in the late 1930's thru early 1950's, so my operation can never be 100% hands-free. I'm referring to uncoupling the cars from the train, and locking them onto the dumper so that only the coal falls out during the tipping process.
Over the past 18 years, I've believed I would have to do major surgery on the mill scenery if I ever wanted to make that thing rotate hands-free, so I kept deferring the idea. Fast-forward to late January: I was putting some boxes under the layout in proximity to the dumper, and this time the area beneath it didn't seem as congested as it had before. I started envisioning ways I could fit a set of dowels below the layout surface to support it. And I also discovered that the layout surface immediately past the 'exit' end of the dumper was an 18"x10" plank held down by wood screws; this wouldn't require massive amounts of cutting to remove, just undo the screws and lift it out.
Knowing that mechanizing the dumper was doable, I started trying to figure out ways to spin the supporting dowels that would make the structure rotate. During a phone conversation with my friend Keith, I learned of an incredibly simple approach: Rather than trying to use a set of gears so a motor could spin both dowels, I could just acquire two cheap identical motors with reduction gears already installed, one for each dowel. I would cover the dowels with neoprene rubber hose, and also use that to connect each motor shaft to a dowel. I perused several candidate motors on Amazon, noted their top rotation speeds, then did the math to determine the target RPM range.
I wound up getting a pair of these guys:
https://www.amazon.com/BQLZR-Gear-Box-Stabilivolt-Electric-Replacement/dp/B00HDDXBEY/ref=asc_df_B00HDDXBEY/?tag=hyprod-20&linkCode=df0&hvadid=312106042452&hvpos=&hvnetw=g&hvrand=307760750817765631&hvpone=&hvptwo=&hvqmt=&hvdev=m&hvdvcmdl=&hvlocint=&hvlocphy=9051899&hvtargid=pla-492604452120&psc=1&tag=&ref=&adgrpid=62821668875&hvpone=&hvptwo=&hvadid=312106042452&hvpos=&hvnetw=g&hvrand=307760750817765631&hvqmt=&hvdev=m&hvdvcmdl=&hvlocint=&hvlocphy=9051899&hvtargid=pla-492604452120
They were $16 apiece, rated for 12 volts, with a no-load rotation speed of 25 RPM. A trip to the nearest Home Depot for some 5/16" diameter dowels dowels, Advance Auto Parts for the neoprene fuel hose material (5/16" inside diameter), and some 1/4" thick plywood pieces from the scrap box - I now had all the raw materials necessary to build a drive mechanism.
Here is what I eventually kluged together:
I added some neoprene over the dowels, then tested it out by connecting it to an old MRC Tech II power pack.
I shot a 36-second video of the test using my cell phone [sorry about the shaky image, didn't have a tripod]. The forum software doesn't let me directly embed it in the message - so to view it you'll have to click this link: http://ironbelt.net/images/DumperFirstTrialRun.mp4
I used a solid pseudo-load of "coal" for the test in order to avoid spilling Black Beauty sand all over the workbench.
...and that is all I have time to type-in tonight! My next post will describe the process of making it fit under the layout.
Over the past 18 years, I've believed I would have to do major surgery on the mill scenery if I ever wanted to make that thing rotate hands-free, so I kept deferring the idea. Fast-forward to late January: I was putting some boxes under the layout in proximity to the dumper, and this time the area beneath it didn't seem as congested as it had before. I started envisioning ways I could fit a set of dowels below the layout surface to support it. And I also discovered that the layout surface immediately past the 'exit' end of the dumper was an 18"x10" plank held down by wood screws; this wouldn't require massive amounts of cutting to remove, just undo the screws and lift it out.
Knowing that mechanizing the dumper was doable, I started trying to figure out ways to spin the supporting dowels that would make the structure rotate. During a phone conversation with my friend Keith, I learned of an incredibly simple approach: Rather than trying to use a set of gears so a motor could spin both dowels, I could just acquire two cheap identical motors with reduction gears already installed, one for each dowel. I would cover the dowels with neoprene rubber hose, and also use that to connect each motor shaft to a dowel. I perused several candidate motors on Amazon, noted their top rotation speeds, then did the math to determine the target RPM range.
I wound up getting a pair of these guys:
https://www.amazon.com/BQLZR-Gear-Box-Stabilivolt-Electric-Replacement/dp/B00HDDXBEY/ref=asc_df_B00HDDXBEY/?tag=hyprod-20&linkCode=df0&hvadid=312106042452&hvpos=&hvnetw=g&hvrand=307760750817765631&hvpone=&hvptwo=&hvqmt=&hvdev=m&hvdvcmdl=&hvlocint=&hvlocphy=9051899&hvtargid=pla-492604452120&psc=1&tag=&ref=&adgrpid=62821668875&hvpone=&hvptwo=&hvadid=312106042452&hvpos=&hvnetw=g&hvrand=307760750817765631&hvqmt=&hvdev=m&hvdvcmdl=&hvlocint=&hvlocphy=9051899&hvtargid=pla-492604452120
They were $16 apiece, rated for 12 volts, with a no-load rotation speed of 25 RPM. A trip to the nearest Home Depot for some 5/16" diameter dowels dowels, Advance Auto Parts for the neoprene fuel hose material (5/16" inside diameter), and some 1/4" thick plywood pieces from the scrap box - I now had all the raw materials necessary to build a drive mechanism.
Here is what I eventually kluged together:
I added some neoprene over the dowels, then tested it out by connecting it to an old MRC Tech II power pack.
I shot a 36-second video of the test using my cell phone [sorry about the shaky image, didn't have a tripod]. The forum software doesn't let me directly embed it in the message - so to view it you'll have to click this link: http://ironbelt.net/images/DumperFirstTrialRun.mp4
I used a solid pseudo-load of "coal" for the test in order to avoid spilling Black Beauty sand all over the workbench.
...and that is all I have time to type-in tonight! My next post will describe the process of making it fit under the layout.